Case Study: NE, USA

EnerCorp was called into a project, mid-week, with a report of a sanded-off wellhead. The client’s nearby well had a ‘zipper frac,’ and communicated with a preexisting well that had been on an artificial lift. EnerCorp arrived on location at 8:00am, bled off and rigged out the preexisting flowline.